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低渗透油藏改善开发效果研究与实践
引用本文:李晓良,王庆魁,王学立,吕中锋,季岭. 低渗透油藏改善开发效果研究与实践[J]. 桂林工学院学报, 2009, 29(2)
作者姓名:李晓良  王庆魁  王学立  吕中锋  季岭
作者单位:1. 油气藏地质及开发工程国家重点实验室,成都理工大学,成都,610059;大港油田第三采油厂,河北,沧州,061035
2. 大港油田第三采油厂,河北,沧州,061035
基金项目:中国石油大港油田分公司重点科技项目 
摘    要:舍女寺油田孔二段油藏空气渗透率26.7×10-3 μm2,开发过程中存在储层物性差、注水困难、注采井网不完善、油藏低速低效开采等问题.为此,开展了孔二段低渗油藏改善开发效果的4项研究,即提高水驱控制程度、合理驱动压力梯度、小井距加密提高连通程度和非主流线井压裂.实施后舍女寺油田孔二段油藏采油速度从0.81%上升到0.92%,最终采收率从14.8%提高到26.1%,增加可采储量38×104 t,为同类型油藏提供了改善开发效果的技术对策.

关 键 词:低渗透油藏  开发效果  小井距  连通程度  压裂改造

Study on Improving Low Permeability Oil Reservoir
LI Xiao-liang,WANG Qing-kui,WANG Xue-li,LU Zhong-feng,JI Ling. Study on Improving Low Permeability Oil Reservoir[J]. Journal of Guilin University of Technology, 2009, 29(2)
Authors:LI Xiao-liang  WANG Qing-kui  WANG Xue-li  LU Zhong-feng  JI Ling
Affiliation:1.State Key Laboratory of Oil and Gas Reservoir Geology and Exploitation;Chengdu University of Technology;Chengdu 610059;China;2.Third Oil Production Plant;Dagang Oilfield;Cangzhou 061035;China
Abstract:In the low permeability reservoir,there exist higher pressure in water injecting,poor injecting and discovery well-pattern,low speed and low effective in the development of Member 2 of Kongdian Formation in Shenvsi Oilfield.In order to solve these problems,four suggestions are proposed to improve the development in the low permeability oil reservoir,such as improving the degree of water flooding,optimizing technique of the reasonable driving pressure gradient,infilling well spacing and increasing the interc...
Keywords:low permeability oil reservoir  recoverable reserve  infilling well spacing  connectivity degree  fracturing
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