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耐高温微生物驱油提高低渗透油藏采收率先导性试验
引用本文:尹志青,赵明宸,高进锋,杨峰,王庆,张兴,单俊杰.耐高温微生物驱油提高低渗透油藏采收率先导性试验[J].石油地质与工程,2002,16(5):21-23.
作者姓名:尹志青  赵明宸  高进锋  杨峰  王庆  张兴  单俊杰
作者单位:1. 胜利油田有限公司东辛采油厂,山东东营,257094
2. 胜利石油管理局胜东社区管理中心
摘    要:胜利油田东辛高温低渗透油藏含蜡高,常温微生物无法存活,针对这一问题,引进美国NPC公司耐高温菌种,在Y6-16井组开展高温低渗油藏微生物驱油提高采收率研究和现场试验。施工后Y6-16井日增注52m3,表皮系数由施工前的2.069减小为施工后的-6.31,油层污染得到较好改善;原油含蜡量、胶质沥青质含量降低,轻质组分增加,重质组分降低;井组采收率提高5.09个百分点。

关 键 词:微生物驱油  低渗透油藏  采收率  试验
文章编号:1006-4095(2002)05-0021-02
修稿时间:2002年4月2日

Pilot of High Temperature Resistant Microbial Flooding in Reservoirs with Low Permeability
YIN Zhi-qing et a l.Pilot of High Temperature Resistant Microbial Flooding in Reservoirs with Low Permeability[J].Petroleum Geology and Engineering,2002,16(5):21-23.
Authors:YIN Zhi-qing et a l
Abstract:Normal temperature microbial cannot survive in Dongxin low perme ability reservoirs due to its high temper-ature and high wax contents.High tem perature resistant microbial specie incubated by American NPC Company was impor ted to solve this problem.Pilot of microbial flooding of reservoirs with high t emperature and low permeability was carried out in Well group Y6-16.Single well injection increased52m 3 ,skin coefficient lowered from2.069to-6.31,and reservoir contam ination was improved.Wax and gel and asphalt contents in the produced crude oil lowered,light hydrocarbon contents increased,heavy hydrocarbon content lowe red and recovery factor increased5.09%.
Keywords:microbial flooding  low permeability reservoir  recovery factor  experiment  
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