首页 | 官方网站   微博 | 高级检索  
     

某飞控部件连接螺柱断裂分析
引用本文:何胜强,章惠君. 某飞控部件连接螺柱断裂分析[J]. 理化检验(物理分册), 2012, 0(3): 200-202,205
作者姓名:何胜强  章惠君
作者单位:中国空空导弹研究院
摘    要:通过断口分析、金相检验和硬度测试查明了连接螺柱断裂失效的机理和过程,并结合有限元分析得出连接螺柱在疲劳载荷下的动响应,对失效的原因做出判断。结果发现:连接螺柱疲劳抗力不足以及飞控部件承力构件布局不合理是造成连接螺柱断裂的主要原因。最后,从工艺和结构方面有针对性地采取了改进和预防措施,避免同类失效的再次发生,达到改进产品质量、延长使用寿命、提高服役安全性和可靠性的目的。

关 键 词:飞控部件  连接螺柱  断口分析  有限元分析

Fracture Analysis of Joint Stud in a Flight Control Part
HE Sheng-qiang,ZHANG Hui-jun. Fracture Analysis of Joint Stud in a Flight Control Part[J]. Physical Testing and Chemical Analysis Part A:Physical Testing, 2012, 0(3): 200-202,205
Authors:HE Sheng-qiang  ZHANG Hui-jun
Affiliation:(China Airborne Missile Academy,Luoyang 471009,China)
Abstract:The fracture mechanism and process of joint stud were analyzed by means of fracture analysis,metallographic examination and hardness testing.The dynamic responses of connections of stud under fatigue loading were obtained by combining finite element analysis.The results showed that the fracture reason of joint stud was meanly due to the lack of fatigue resistance of joint stud and the unreasonably arranged distribution of flight control component.Finally,the improvement and preventive measures in techniques and structures were made,which kept the failure from happen.The resulted products were then better in quality,prolonged in life cycle,safer and more reliable.
Keywords:flight control part  joint stud  fracture analysis  finite element analysis
本文献已被 CNKI 维普 等数据库收录!
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司    京ICP备09084417号-23

京公网安备 11010802026262号