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钻盐膏层及高压气层的高密度钻井液
引用本文:肖俊峰,胡金鹏,冯兴武,殷宏飞,何涛.钻盐膏层及高压气层的高密度钻井液[J].石油地质与工程,2000(5).
作者姓名:肖俊峰  胡金鹏  冯兴武  殷宏飞  何涛
作者单位:河南石油勘探局(肖俊峰,胡金鹏,冯兴武,殷宏飞),塔里木石油会战指挥部(何涛)
摘    要:KL—2井是塔里木盆地克拉苏构造山前构造的一口预探井,钻探过程中,盐膏层及高压气压易出现缩径、井涌、井漏及卡钻等复杂情况,采用聚磺氯化钾钻井液体系,密度控制在 1.75~1.809/cm3和2.20~2.40g/Cm3平衡地层压力,较好地解决了钻探过程中出现的各种复杂情况。

关 键 词:盐膏层  高压  气层  高密度  钻井液  井溢  井漏  小井眼

High-density Drilling Fluid for Drilling Salt -gypsum Layers and Overpressured Gas Layers
XIAO Jun -feng,HU Jin -peng et al.High-density Drilling Fluid for Drilling Salt -gypsum Layers and Overpressured Gas Layers[J].Petroleum Geology and Engineering,2000(5).
Authors:XIAO Jun -feng  HU Jin -peng
Abstract:Well KL-2 is a wildcat well drilled in the predmont structure of Kelasu structure in Tarim basin. Complex situations such as undergauge, overflow, lost circulation and differential sticking are easy to occurs when drilling in salt-gypsum layers and overpressured gas layers.These problems are solved through using polysulfonate potassium chloride drilling fluid and keeping drilling fluid density at 1.75 to 1.80g/cm3 in halite intervals and at 2.20 to 2.40 g/cm3 in overpressured gas intervals to balance formation pressure.
Keywords:salt-gypsum layer  high density drilling fluid  overflow  lost circulation  slilnho4  
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