共查询到20条相似文献,搜索用时 78 毫秒
1.
2.
3.
基于DSP的电液伺服机构控制 总被引:4,自引:0,他引:4
针对电液位置伺服控制,以TMS320C2812 DSP为平台,采用模糊PID控制方法,阐述了用DSP实现电液压伺服控制器的设计。试验结果表明,DSP能很好实现实时控制算法,使得伺服控制器能很好地实现实时控制,系统具有良好的动态品质和稳态性能,满足高精度位置伺服控制的要求。 相似文献
4.
5.
6.
7.
8.
由于导弹电液伺服机构具有小阻尼、时变性等特点,而且具有不确定性,致使无法得到精确的数学模型。为了保证实际设计过程中控制算法的有效性,采用模糊滑模控制算法。利用Simulink和RTW工具箱,直接在物理硬件上建立实时数字仿真模型,方便快速得到试验结果。实现了对伺服机构的快速半实物仿真,并快速验证了算法的有效性,提高了控制系统的设计效率。 相似文献
9.
为测试氟橡胶密封圈在某装甲车油气弹簧的液压驱动系统中的适用性,参照GB/T1690-2010《硫化橡胶或热塑性橡胶耐液体试验方法》,通过试验分析氟橡胶密封圈与油气弹簧常用的46号抗磨减震液、10号航空液压油和4609减震液的相容性。结果表明:氟橡胶密封圈在3种液压液及其混合油中的体积变化率都是负值,最大体积收缩率都大于4%,不满足GB/T14832-2008标准的要求。氟橡胶并不适用于油气弹簧采用的3种用油,建议将氟橡胶材料更换为腈橡胶材料。 相似文献
11.
12.
13.
Current researches show that mechanical deformation of seal ring face makes fluid film clearance decrease at high pressure side, thus a divergent clearance is formed and face wear occurs more seriously at the high pressure side than that on the low pressure side. However, there is still lack of published experimental works enough to prove the theoretical results. In this paper, a spiral groove dry gas seal at high pressures is experimentally investigated so as to prove the face wear happened at the high pressure side of seal faces due to the face mechanical deformation, and the wear behavior affected by seal ring structure is also studied. The experimental results show that face wear would occur at the high pressure side of seal faces due to the deformation, thus the leakage and face temperature increase, which all satisfies the theoretical predictions. When sealed pressure is not less than 5 MPa, the pressure can provide enough opening force to separate the seal faces. The seal ring sizes have obvious influence on face wear. Face wear, leakage and face temperature of a dry gas seal with the smaller cross sectional area of seal ring are less than that of a dry gas seal with bigger one, and the difference of leakage rate between these two sizes of seal face width is in the range of 24%–25%. Compared with the effect of seal ring sizes, the effect of secondary O-ring seal position on face deformation and face wear is less. The differences between these two types of dry gas seals with different secondary O-ring seal positions are less than 5.9% when the rotational speed varies from 0 to 600 r/min. By linking face wear and sealing performance changes to the shift in mechanical deformation of seal ring, this research presents an important experimental method to study face deformation of a dry gas seal at high pressures. 相似文献
14.
15.
16.
17.
设计了主要用于飞机刹车系统的2D压力伺服阀,其阀芯具有移动自由度和旋转自由度。将波登管作为压力反馈单元输出反馈力矩,与拨杆拨叉联动,实现与主阀的闭环力反馈,从而保持其压力输出恒定;分析了波登管力反馈机构的传力方式,建立了2D压力伺服阀的数学模型,仿真分析了主阀的静动态特性;设计了样机实验方案并搭建实验平台,实验结果表明:2D压力伺服阀输出压力与旋转电磁铁输入电流基本成线性关系,输出压力的阶跃响应时间约为18 ms。实验结果与仿真分析结果基本一致。 相似文献
18.
变工况条件下机械密封端面膜压实验研究 总被引:1,自引:0,他引:1
通过机械密封端面稳定实验,研究热油泵机械密封在工况变化时端面膜压变化,分析相同转速、相同温度和不同压力以及相同压力、相同温度和不同转速2种工况下机械密封端面膜压实验结果,并与变工况机械密封理论计算结果进行比较。实验结果与变工况机械密封理论计算结果吻合。工况变化瞬时,密封端面液膜失稳导致汽化半径瞬时增大,发生闪蒸,由于闪蒸端面压力瞬时增大,使得端面的开启力大于闭合力,造成机械密封发生开启失效;在持续抽空过程中,密封端面会发生干摩擦,加剧端面磨损。 相似文献
19.
高压机械密封的设计与应用 总被引:3,自引:0,他引:3
从传动机构、结构型式、端面型式、辅助系统和零件选材等方面分析了高压机械密封的技术关键,介绍了性能稳定、寿命长、可用于不同工况的多种高压机械密封产品的设计与介绍现场应用。 相似文献
20.
分析空气滤清器的原始压力损失与螺杆空压机能效的相互关系,得出计算公式和图表,作为评价空气滤清器能效水平的依据;分析和总结现阶段螺杆空压机用空气滤清器原始压力损失的现状,得出有必要建立健全压缩机行业空气滤清器技术准则的结论。 相似文献