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曝气生物滤池处理性能影响因素实验研究
引用本文:张连科.曝气生物滤池处理性能影响因素实验研究[J].云南环境科学,2013(6):54-56.
作者姓名:张连科
作者单位:内蒙古科技大学能源与环境学院,内蒙古包头014010
摘    要:采用上向流曝气生物滤池处理生活污水,考察了气水比、水力负荷、有机负荷、滤料层高度等因素对曝气生物滤池处理性能的影响。结果表明,气水比为5:1时,COD和NH3-N的去除率分别为87.6%和60.1%;水力负荷在0.21—0.86m^3/(m^2·h)的条件下,COD的去除率随水力负荷的增加降幅较小,NH3-N的去除率下降明显;有机负荷在1.15~2.96kg/(m^3·d)的条件下,BAF表现出很好的抗有机负荷冲击能力。BAF对有机物的去除主要发生在滤料层0~70cm段,对NH3-N的硝化主要发生在滤料层40—100cm段。

关 键 词:曝气生物滤池  气水比  水力负荷  有机负荷

The Experimental Study on Influence Factors of Biological Aerated Filter
Affiliation:ZHANG Lian - ke (School of Energy and Environment, Inner Mongolia University of Science and Technology, Baotou Inner Mongolia 014010 China)
Abstract:An up -flow biological aerated filter (UBAF) was used to treat domestic wastewater. The influence of gas - water ratios, hydraulic loading, organic loading and filter height on the removal efficiency of the biological aerated filter was investigated. The results showed that when the gas - water ratios was 5 : 1, the removal rates of COD and NH3 - N was respectively 87.6% and 60. 1% ; when the hydraulic loading was 0. 21 - 0.86 m3/ ( m2 . h), the removal rate of COD was gradually decreased with increasing hydraulic loading, the removal rates of NH3 - N was significantly decreased; when the organic loading was 1. 15 -2.96 kg/ (m3 . d) , the BAF process showed the strong resistance to the sudden change of organic loading. The COD was removed mainly in the layer from 0 to 70era thickness, and nitrogen from 40 - 100cm thickness.
Keywords:biological aerated filter  gas -water ratio  hydraulic loading  organic loading
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