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大斜度井有杆泵举升配套技术的研究与应用
引用本文:刘丙生,徐建礼,程正全.大斜度井有杆泵举升配套技术的研究与应用[J].石油机械,2009,37(11).
作者姓名:刘丙生  徐建礼  程正全
作者单位:胜利油田分公司采油工艺研究院
基金项目:中石化胜利油田分公司专利实施项目"稠油开采配套专利技术推广"(YZ0701).该技术中采用的偏置阀式抽油泵已获国家实用新型专利;专利号:ZL200520135895.6 
摘    要:针对常规有杆泵在大斜度井中举升时,存在偏磨导致管杆断脱严重、杆柱下行阻力大和泵效低的问题,开发了新型有杆泵抽油配套技术。该配套技术采用偏置阀式抽油泵、钢质连续抽油杆和旋转井口装置等部件,并配套组成了大斜度井有杆泵举升工艺管柱。经500余口井的现场应用表明,采用该配套技术,平均泵效比常规抽油泵提高了5%~10%,检泵周期延长6月以上,举升效果明显。

关 键 词:斜井  偏置阀式抽油泵  钢质连续抽油杆  旋转井口装置

Research and application of the matching technology for rod pump lift in high-inclination wells
Liu Bingsheng,Xu Jianli,Cheng Zhengquan.Research and application of the matching technology for rod pump lift in high-inclination wells[J].China Petroleum Machinery,2009,37(11).
Authors:Liu Bingsheng  Xu Jianli  Cheng Zhengquan
Abstract:In light of the problem that the lift of the conventional sucker rod pump in high-angle wells gives rise to eccentric wear which will cause the serious parting of the rod,much resistance for the rod string to go down and low pump efficiency,a kind of new-type matching technology for sucker rod pump was developed.The technology adopts biased-valve oil well pump,coiled steel rod and rotary wellhead parts,which form the technological pipe string for the lift of the sucker rod pump in highly-deviated wells.The field application in over 500 wells shows that the matching technology can improve average pump efficiency by 5%~10%,compared with that of ordinary oil well pumps.The pump inspection cycle is lengthened over 6 months.The lifting effect is obvious.
Keywords:deviated well  biased-valve oil well pump  coiled steel sucker rod  rotary wellhead
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