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A/O除磷工艺丝状菌污泥膨胀的研究
引用本文:马金明,李冬,吴迪,张功良,张杰.A/O除磷工艺丝状菌污泥膨胀的研究[J].中国给水排水,2012,28(7):38-42.
作者姓名:马金明  李冬  吴迪  张功良  张杰
作者单位:1. 北京工业大学水质科学与水环境恢复工程北京市重点实验室,北京,100124
2. 北京工业大学水质科学与水环境恢复工程北京市重点实验室,北京100124;哈尔滨工业大学城市水资源与水环境国家重点实验室,黑龙江哈尔滨150090
基金项目:国家自然科学基金资助项目(50878003);北京市自然科学基金资助项目(8092006);城市水资源与水环境国家重点实验室开放基金资助项目(QAK201005);国家水体污染控制与治理科技重大专项(2008ZX07208-003-003、2008ZX07208-005-003、2009ZX07424-001、2009ZX07424-002-003、2009ZX07424-005)
摘    要:丝状菌污泥膨胀是影响活性污泥法高效、稳定运行的重要因素。采用A/O生物除磷工艺中试装置处理实际生活污水,分析了污泥膨胀发生的原因及恢复系统性能的方法。结果显示,长期曝气不均匀是导致丝状菌污泥膨胀的重要原因,通过调控系统运行参数可以有效控制由低DO值或者高负荷引起的丝状菌污泥膨胀。当发生污泥膨胀后,首先降低负荷至0.45 kgCOD/(kgMLSS.d),调节回流比为83%,同时控制好氧池各段的DO分别为1.5、1.0、1.0 mg/L以淘汰丝状菌,在SVI值降至200 mL/g以下后继续降低回流比至53%,同时降低曝气量以形成1.0、0.5、0.5 mg/L的DO浓度梯度。采取上述调控措施后,SVI值由569.8 mL/g降至150 mL/g以下,污泥性状得以恢复;同时出水COD和TP分别在50、0.5 mg/L以下,去除率分别约为85%、95%。

关 键 词:丝状菌污泥膨胀  A/O生物除磷工艺  污泥负荷  DO

Study on Filamentous Sludge Bulking in A/O Phosphorus Removal Process
MA Jin-ming , LI Dong , WU Di , ZHANG Gong-liang , ZHANG Jie.Study on Filamentous Sludge Bulking in A/O Phosphorus Removal Process[J].China Water & Wastewater,2012,28(7):38-42.
Authors:MA Jin-ming  LI Dong  WU Di  ZHANG Gong-liang  ZHANG Jie
Affiliation:1,2(1.Key Laboratory of Beijing for Water Quality Science and Water Environment Recovery Engineering,Beijing University of Technology,Beijing 100124,China;2.State Key Laboratory of Urban Water Resource and Environment,Harbin Institute of Technology,Harbin 150090, China)
Abstract:Filamentous sludge bulking is an important factor influencing the operation of activated sludge process.A/O process was used to treat domestic sewage,and the reason and recovery of sludge bulking were studied.The results showed that long-term fluctuation of aeration was the key reason of filamentous sludge bulking,and proper regulation of running parameters could effectively control filamentous sludge bulking caused by low DO or high loading rate.When filamentous sludge bulking occurred,the loading rate was reduced to 0.45 kgCOD/(kgMLSS·d),the reflux ratio was adjusted to 83%,and the DO concentrations in different stages of aerobic tank were controlled at 1.5 mg/L,1.0 mg/L and 1.0 mg/L in order to eliminate filamentous bacteria.When the value of SVI was below 200 mL/g,the reflux ratio was decreased to 53% and the aeration rate was reduced to form a DO gradient of 1.0 mg/L,0.5 mg/L and 0.5 mg/L.After these measures were taken,the value of SVI decreased from 569.8 mL/g to below 150 mL/g,and sludge characteristics recovered.The effluent concentrations of COD and TP were below 50 mg/L and 0.5 mg/L,with removal rates 85% and 95%,respectively.
Keywords:filamentous sludge bulking  A/O phosphorus removal process  sludge loading  dissolved oxygen
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