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三板溪主坝面板破损前后应变应力分析
引用本文:朱锦杰,李涛,杜雪珍.三板溪主坝面板破损前后应变应力分析[J].大坝与安全,2009(6).
作者姓名:朱锦杰  李涛  杜雪珍
作者单位:国家电力监管委员会大坝安全监察中心,浙江,杭州,310014
摘    要:通过分析三板溪主坝面板应变应力监测资料,发现一、二期面板压应力很大,分期浇筑接缝处承受8~15 MPa的压应力,在蓄水期水位快速上升过程中,面板挤压破损,需降低水位检查修补,影响工程安全和效益。面板修补后虽取得了一定效果,但面板高压应力的情况仍存在,应加强监测和现场巡查,密切关注渗漏量等的变化,保证大坝的安全运行。

关 键 词:三板溪主坝  面板  挤压破损  应变应力  分析

Analysis on stress and strain before and after the face-slab damage of Sanbanxi dam
ZHU Jin-jie,LI Tao,DU Xue-zhen.Analysis on stress and strain before and after the face-slab damage of Sanbanxi dam[J].Large Dam & Safety,2009(6).
Authors:ZHU Jin-jie  LI Tao  DU Xue-zhen
Affiliation:ZHU Jin-jie; LI Tao and DU Xue-zhen Large Dam Safety Supervision Center of SERC;
Abstract:By analysis on the monitoring data of face-slab stress and strain,huge compressive stress was found on the face-slab,and the compressive stress at the joints was 8~15 MPa.In the process of storage water level rising,face-slab damage happened which exerted bad influence on the safety and profit of the project.Although rehabilitation,high compressive stress didn t disap-pear which called for closer monitoring.Only in this way,dam safety can be guaranteed.
Keywords:Sanbanxi dam  face-slab  extrusion damage  stress and strain  analysis  
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