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单家寺油田单10块稠油油藏剩余油挖潜措施
引用本文:朱孟高,沈国华,谢风猛,刘建,郭卫忠.单家寺油田单10块稠油油藏剩余油挖潜措施[J].油气地质与采收率,2003,10(4):53-54.
作者姓名:朱孟高  沈国华  谢风猛  刘建  郭卫忠
作者单位:胜利油田有限公司滨南采油厂
摘    要:利用油藏数值模拟、剩余油饱和度监测、钻密闭取心井、常规油藏工程分析等手段,寻找单家寺油田单10块稠油热采油藏剩余油饱和度的相对富集区。通过新钻井、老井侧钻、深度调剖、注氮气等技术进行剩余油挖潜,油藏开发效果得到明显改善。综合递减率下降10.0%,采收率提高2.94%,油汽比上升0.11。对单10块剩余油研究拓展了多轮次吞吐稠油油藏的挖潜方向,对同类油藏改善开发效果和提高采收率具有参考价值。

关 键 词:单家寺油田  单10块  稠油油藏  剩余油  挖潜措施  多轮次吞吐挖潜
文章编号:1009-9603(2003)04-0053-02
修稿时间:2003年1月2日

Measures of tapping the potential of remaining oil in heavy oil reservoir of Shan 10 block in Shanjiasi oilfield
Zhu Menggao,Shen Guohua,Xie Fengmeng et al..Measures of tapping the potential of remaining oil in heavy oil reservoir of Shan 10 block in Shanjiasi oilfield[J].Petroleum Geology and Recovery Efficiency,2003,10(4):53-54.
Authors:Zhu Menggao  Shen Guohua  Xie Fengmeng
Abstract:Relative enrichment area of remaining oil saturation in heavy oil reservoir by thermal recovery of Shan 10 block in Shanjiasi oilfield is looked for using the measures of reservoir numerical simulation, remaining oil saturation monitoring, drilling pressure cored well , normal reservoir engineering analysis. Reservoir development effect is improved obviously by tapping the potential of the remaining oil with the technologies of drilling new well, sidetrack drilling of old wells, deep profile control, nitrogen injection. Composite decline rate decreased 10. 0% , recovery efficiency enhanced 2.94% and oil-steam ratio raised 0. 11. The research of the remaining oil in Shan 10 block enriched the direction in tapping potential of multicyclic steam stimulation in heavy oil reservoir, and has reference value for improving the development results and enhancing recovery efficiency in the same type of the oil reservoir.
Keywords:heavy oil reservoir  remaining oil distribution  tapping potential by multicyclic steam stimulation  Shanjiasi oilfield  
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