首页 | 官方网站   微博 | 高级检索  
     

高有机物污染原水深度处理工艺选择和运行优化
引用本文:周建平,许龙,芮旻,沈飚,富良.高有机物污染原水深度处理工艺选择和运行优化[J].给水排水,2012,38(1):17-20.
作者姓名:周建平  许龙  芮旻  沈飚  富良
作者单位:1. 上海市政工程设计研究总院(集团)有限公司,上海,200092
2. 平湖市水务投资(集团)有限公司,平湖,314200
摘    要:P市地表原水受到有机物污染,水中CODMn经常高达10mg/L以上,为此,在G水厂的扩建工程中,采用了两级臭氧—生物活性炭深度处理工艺,以保证出水水质安全。水厂运行结果表明,在活性炭吸附饱和后,一级炭池出水CODMn仍有3~5mg/L,需二级臭氧—生物活性炭处理才能使出厂水CODMn小于3mg/L。当前后臭氧分级投加比例为3∶2时,有机物的去除率最高。

关 键 词:高有机物污染原水  深度处理  两级臭氧—生物活性炭  优化运行

Process selection and optimization of the advanced treatment for the high organic polluted raw water
Zhou Jianping , Xu Long , Rui Min , Shen Biao , Fu Liang.Process selection and optimization of the advanced treatment for the high organic polluted raw water[J].Water & Wastewater Engineering,2012,38(1):17-20.
Authors:Zhou Jianping  Xu Long  Rui Min  Shen Biao  Fu Liang
Affiliation:1.Shanghai Municipal Engineering Design Institute(Group) Co.,Ltd.,Shanghai 200092,China; 2.Pinghu Water Supply(Group) Co.,Ltd.,Pinghu 314200,China)
Abstract:The raw water of P City was polluted by organic pollutants and the CODMn of the raw water was often above 10 mg/L.To ensure the safety of the drinking water,two-stage O3-BAC was used in G Water Treatment Plant extension project.The results showed that with the absorb saturation of the GAC,the CODMn in the effluent of the first stage O3-BAC still remained at 3~5 mg/L,which made the second stage O3-BAC needed to lower the CODMn in finished water to less than 3 mg/L.When the O3 dosage ratio between the first and the second stage was 3∶2,the highest organic removal rate could be achieved.
Keywords:High organic polluted raw water  Advanced treatment  Two stage O3-BAC  Optimized operation
本文献已被 CNKI 万方数据 等数据库收录!
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司    京ICP备09084417号-23

京公网安备 11010802026262号